石油炼制与化工
• 加工工艺 • 上一篇 下一篇
潘罗其1,颜刚1,聂白球1,崔守业2
收稿日期:
修回日期:
出版日期:
发布日期:
通讯作者:
Received:
Revised:
Online:
Published:
摘要: 介绍了巴陵石化公司在MIP工艺装置上回炼轻柴油以增产高辛烷值汽油的应用结果。当柴油轻馏分油选择性再裂化时,柴油产率平均减少1.41个百分点,目的产物(汽油+液化气)产率平均增加1.16个百分点,汽油研究法辛烷值略有增加,马达法辛烷值约增加0. 5个单位,通过将劣质柴油轻馏分选择性再裂化可以实现增产高辛烷值汽油的目的。
关键词: MIP, 高辛烷值汽油, 回炼, 催化裂化, 工业应用
Abstract: MIP process for enhancing high octane gasoline production was commercially applied at SINOPEC Baling Petrochemical Company, in this process light diesel fraction was recycled and cracked. Application results showed that the yield of light diesel fraction decreased 1.41 percentage points, the yield of target products (gasoline and LPG) increased 1.16 percentage points, gasoline RON increased slightly and MON increased 0.5 units, which indicating that the yield of high octane gasoline could be increased by selectively cracking the low quality light diesel fraction.
Key words: MIP, high octane gasoline, recracking, catalytic cracking, commercial application
潘罗其1 ,颜刚1 ,聂白球1 ,崔守业2 . MIP装置柴油轻馏分回炼增产高辛烷值汽油的工业实践[J]. 石油炼制与化工, doi: .
0 / / 推荐
导出引用管理器 EndNote|Ris|BibTeX
链接本文: http://www.sylzyhg.com/CN/
http://www.sylzyhg.com/CN/Y2011/V42/I1/33