石油炼制与化工

• 节能减排 • 上一篇    下一篇

蒸汽管网节能-冷凝水回收技术在炼油厂的应用

权亚文1,白小明1,倪晓斌1,黄传峰2   

  1. 1. 陕西延长石油(集团)有限责任公司榆林炼油厂
    2. 陕西延长石油(集团)公司研究院;陕西延长石油集团榆林炼油厂
  • 收稿日期:2011-01-21 修回日期:2011-04-07 出版日期:2011-09-12 发布日期:2011-09-12
  • 通讯作者: 权亚文

APPLICATION OF STEAM PIPE NETWORK OPTIMIZATION FOR CONDENSED WATER RECOVERY IN REFINERY

  • Received:2011-01-21 Revised:2011-04-07 Online:2011-09-12 Published:2011-09-12

摘要: 针对陕西延长石油集团榆林炼油厂疏水系统和凝结水回收水质等方面存在的蒸汽泄漏严重、冷凝水回收少、水质差难以达到锅炉等用水要求的问题。采用背压回水与加压回水相结合的蒸汽管网节能技术,将所有凝结水回收并精处理,处理后的凝结水送至蒸汽动力装置进行重复使用,节约了大量蒸汽,对改善低温余热的平衡及生产装置的稳定运行具有重要的意义。

关键词: 蒸汽管网, 冷凝水, 回收

Abstract: Due to the imperfect steam trap system, serious leakage of steam, less recovery of condensed water happened in Yulin refinery, and the poor quality condensed water could not be used as boiler make-up water as well. By adopting energy saving technology of steam pipe network, which included a combination of back pressure return and pressurized backwater, the condensed water was fully recovered and after fine treatment, it could be used as boiler make-up water. Since then, steam and water resource were saved, the utilization of low temperature heat was improved, operations were stable and production cost was reduced in some extent.

Key words: steam pipe network, condensed water, recovery