›› 2017, Vol. 48 ›› Issue (6): 25-29.

• 催化剂 • 上一篇    下一篇

NNI-1型C5/C6异构化催化剂再生性能

杨成艺   

  1. 中国石化海南炼油化工有限公司
  • 收稿日期:2016-11-30 修回日期:2017-01-10 出版日期:2017-06-12 发布日期:2017-05-24
  • 通讯作者: 杨成艺 E-mail:yangcy.hnlh@sinopec.com

REGENERATION PERFORMANCE OF C5/C6 ISOMERIZATION CATALYST NNI-1

  • Received:2016-11-30 Revised:2017-01-10 Online:2017-06-12 Published:2017-05-24

摘要: 介绍了中国石化海南炼油化工有限公司200 kt/a C5/C6异构化装置NNI-1型载钯分子筛催化剂器外再生前后的工业运行情况。异构化催化剂再生前共运行3个周期,前两个周期催化剂共运行7年,反应器入口温度保持不高于250 ℃,床层温升10~15 ℃,生成油RON大于78、提升约6个单位,C5异构化率平均值为58.15%,C6异构化率平均值为73.32%,2,2-二甲基丁烷选择性平均值为14.78%,催化剂表现出了优异的活性和稳定性。进入第三个运行周期后,催化剂活性下降明显加快,运行末期,生成油RON提升不到1个单位,C5异构化率降至43.96%,C6异构化率降至51.42%,2,2-二甲基丁烷选择性降至2.42%,催化剂性能已远远不能满足生产需要。于2015年进行了催化剂的器外再生,再生后近1年的运行数据表明,在装置高负荷运行工况下,反应器入口温度保持在240.0 ℃,生成油RON大于78、提升7.1个单位,床层温升18.7 ℃,C5异构化率为60.87%,C6异构化率为70.22%,2,2-二甲基丁烷选择性为15.49%,催化剂再生后,异构化性能明显上升,保持良好的活性和稳定性,可满足生产需要。

关键词: C5/C6烷烃异构, 催化剂, 再生 , 辛烷值

Abstract: The performance of NNI-1 Pd/molecular sieve catalyst applied in 0.2 Mt/a C5/C6 isomerization unit of SINOPEC Hainan Refining & Chemical Co. Ltd.,before and after regeneration was introduced. The NNI-1 catalyst was run for 3 periods and then regenerated ex-situ. The total time of operation for the first and second periods was 7 years. The inlet temperature of isomerization reactor was controlled under 250 ℃, while the temperature rise of catalyst bed was maintained in the range of 10-15 ℃; the RON of isomerized oil reached 78, 6 units higher than the feed; the C5 average isomerization ratio was 58.15%, and C6 average isomerization ratio was 73.32% with a 2,2-dimethylbutane selectivity of 14.78%. While at the EOR of the third period the RON increase of isomerized oil was less than 1 unit; the average isomerization ratio of C5 reduced to 43.96% and isomerization ratio of C6 was 51.42% with a 2,2-dimethylbutane selectivity of 2.42%, indicating that NNI-1 catalyst was no longer meet the needs of production. After regeneration ex-situ, the NNI-1 catalyst was run again for almost one year. In the case of high load operation, the inlet temperature of reactor maintained at 240 ℃, the temperature rise of reactor bed reached 18.7 ℃, the RON of isomerized oil recovered to 78, the average isomerization ratio of C5 recovered to 60.87% and C6 to 70.22% with the 2,2-dimethylbutane selectivity of 15.49%. The performance of the catalyst after regeneration indicates the well recovery in reactivity and stability meets the need of production.

Key words: C5/C6 alkane isomerization, catalyst, regeneration, octane number