石油炼制与化工 ›› 2026, Vol. 58 ›› Issue (7): 151-159.

• 节能减排 • 上一篇    下一篇

硫酸法烷基化装置节能优化与降耗技术研究

牛东会,许楠,曹太吉,向杰,白春海   

  1. 中石化(河南)炼油化工有限公司
  • 收稿日期:2025-12-16 修回日期:2026-01-13 出版日期:2026-07-12 发布日期:2026-06-29
  • 通讯作者: 牛东会 E-mail:1920152722@qq.com

RESEARCH ON ENERGY-SAVING OPTIMIZATION AND CONSUMPTION REDUCTION TECHNOLOGY OF SULFURIC ACID ALKYLATION UNIT

  • Received:2025-12-16 Revised:2026-01-13 Online:2026-07-12 Published:2026-06-29

摘要: 对中石化(河南)炼油化工有限公司200 kt/a硫酸法烷基化装置的生产能耗进行了分析,并针对装置3.5 MPa蒸汽能耗、1.0 MPa蒸汽能耗及电耗大的问题提出相应节能降耗措施。通过对压缩机转速、脱轻烃塔及脱异丁烷塔换热流程进行优化,分别节省3.5 MPa蒸汽和1.0 MPa蒸汽用量13.2 t/h和6.6 t/h,累计降低3.5 MPa和1.0 MPa蒸汽能耗3310.56 MJ/t,共节约蒸汽成本3532.58万元/a;通过优化酸循环泵和烃循环泵变频,每小时分别可节电56.0 kW.h和22.1 kW.h,累计全年节省用电成本47.89万元;通过优化调整装置9台空气冷却器上方32台风扇开启数量和时间,全年节约电量和用电成本分别为1374474 kW.h和89.34万元;通过优化高速间歇运行的新鲜碱液泵开启频次和时长,全年累计节约电量和用电成本分别为3836 kW.h和0.27万元;则在对电耗进行优化时,实施以上3类节电措施后,累计全年可节约电量2062466 kW.h,累计降低电耗108.06 MJ/t,节约用电成本共137.5万元/a。通过以上针对3.5 MPa蒸汽和1.0 MPa蒸汽及电等能耗介质的节能措施的实施,装置累计降低能耗3418.62 MJ/t,创效3670.08万元/a,并为装置进一步节能降耗提供了依据和支撑。

关键词: 硫酸烷基化, 3.5 MPa蒸汽, 1.0 MPa蒸汽, 电, 节能降耗

Abstract: The production energy consumption of the 200 kt/a sulfuric acid alkylation unit of Sinopec Henan Refining & Chemical Co.,Ltd.was analyzed, and corresponding energy-saving and consumption-reducing measures were proposed for the problems of high energy consumption of 3.5 MPa steam, 1.0 MPa steam and electricity of the unit. By optimizing the rotational speed of the compressor, the heat exchange processes of the dehydrocarbon tower and the deisobutane tower, the consumption of 3.5 MPa steam and 1.0 MPa steam was saved by 13.2 t/h and 6.6 t/h, respectively, and the cumulative energy consumption of 3.5MPa and 1.0 MPa steam was reduced by 3310.56 MJ/t, a total of 35325800 yuan was saved in steam costs per year. By optimizing the frequency conversion of the acid circulation pump and the hydrocarbon circulation pump, the electricity consumption can be saved by 56.0 kW.h and 22.1 kW.h per hour,respectively, resultting in annual electricity cost savings amount to 478900 yuan. By optimizing the number and duration of operation for 32 fans above 9 air coolers, the annual electricity consumption and cost savings were 1374474 kW.h and 893400 yuan, respectively. By optimizing the start-up frequency and duration of the fresh alkali liquid pump with high-speed intermittent operation, the cumulative electricity consumption and electricity cost saved throughout the year were 3836 kW.h and 2700 yuan, respectively.Then, when the optimization of power consumption was carried out, through the implementation of the above three types of power-saving measures, the cumulative annual electricity consumption can be saved by 2062466 kW.h, the cumulative electricity energy consumption can be reduced by 108.06 MJ/t, and the total electricity cost saved was 137500 yuan per year.That was to say, through the implementation of the above 3.5MPa and 1.0 MPa steam and electricity energy-saving measures, the device had cumulatively reduced energy consumption by 3418.62 MJ/t, creating an annual benefit of 36700800 yuan, and providing a basis and support for further energy conservation and consumption reduction of the device.

Key words: alkylation catalyzed by sulfuric acid, 3.5MPa steam, 1.0MPa steam, electricity, energy conservation and consumption reduction