石油炼制与化工

• 加工工艺 • 上一篇    下一篇

蜡油催化裂化装置增产柴油的工业试验

王巍慈1,赵伟林2,李晓光2   

  1. 1. 辽宁石油化工大学职业技术学院
    2. 中国石油抚顺石化公司石油二厂
  • 收稿日期:2011-01-28 修回日期:2011-03-31 出版日期:2011-08-12 发布日期:2011-08-12
  • 通讯作者: 王巍慈

COMMERCIAL TRIAL OF ENHANCING DIESEL FUEL YIELD IN A FCC UNIT

WANG Wei-Ci   

  • Received:2011-01-28 Revised:2011-03-31 Online:2011-08-12 Published:2011-08-12
  • Contact: WANG Wei-Ci

摘要: 介绍增产柴油方案在抚顺石化公司催化裂化装置上的应用情况。工业试验结果表明,通过调整反应-再生系统、分馏系统操作参数和选用DMC-2增产柴油催化剂等措施,产品分布得到改善,柴油收率提高3.77百分点,轻质油收率提高1.81百分点,总液收提高1.06百分点,柴汽质量比增加0.10。采取增产柴油方案后,柴油馏程拓宽,十六烷值略有下降;汽油烯烃含量下降,辛烷值基本不变,诱导期延长;对干气和天然气的质量无不良影响;装置能耗降低。总体经济效益每年可增加约3864万元。

关键词: 催化裂化, 柴油, 催化剂, 汽油, 液化气

Abstract: The commercial trial of enhancing diesel fraction yield in the FCC unit of Fushun Petrochemical Company was introduced. The trial results showed that by adopting measures, such as adjusting operation parameters of reaction-regeneration system and fractionation system, using DMC-2 catalyst designed for the increase of diesel yield, the product slates were improved: the yields of diesel fraction and light oils increased 3.77 and 1.81 percentage points, respectively; the mass ratio of diesel to gasoline increase 0.10. As to the qualities of products, since the boiling range of diesel fraction was broadened, its cetane number was slightly lower; gasoline having lower olefin content, longer induction period and unchanged octane number; without negative effect was found on dry gas and LPG. Furthermore, the energy consumption of the unit was reduced. On the whole, a 37.72 million RMB economic benefit could be obtained annually.

Key words: fluid catalytic cracking, diesel fuel, catalyst, gasoline, liquefied petroleum gas