石油炼制与化工 ›› 2013, Vol. 44 ›› Issue (7): 88-92.
• 设备及防腐 • 上一篇 下一篇
于群,李希斌,刘如松,郑拥军
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摘要: 中海石油中捷石化有限公司500 kt/a重油催化裂化装置于2012年6月进行了节能技术改造,并取得成功,突破了现有催化裂化工艺反应温度和剂油比的矛盾,实现了“低温接触、大剂油比”操作思路,使装置产品收率、产品质量、能耗、烟气排放等各项指标达到高标准值,全面满足了重油催化裂化工艺的技术要求。
Abstract: A 500 kt/a RFCC unit was successfully revamped for energy conservation in CNOOC Zhongjie Petrochemical Co.in June, 2012. The technology overcame conventional contradiction between reaction temperature and catalyst/oil ratio, and has realized the idea of operating the FCC unit under low reaction temperature and large catalyst/oil ratio. The product quality and yield, energy consumption and flue gas emission are satisfied with the contract. An additional economic benefit of 62.1 million RMB is gained annually.
于群 李希斌 刘如松 郑拥军. 500 kt/a重油催化裂化装置节能技术改造[J]. 石油炼制与化工, 2013, 44(7): 88-92.
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