石油炼制与化工 ›› 2014, Vol. 45 ›› Issue (4): 68-72.

• 加工工艺 • 上一篇    下一篇

柴油加氢装置扩能改造为石脑油加氢装置的生产实践

薛海锋,吴利军   

  1. 中国石化镇海炼油化工股份有限公司
  • 收稿日期:2013-08-06 修回日期:2013-12-16 出版日期:2014-04-12 发布日期:2014-03-24
  • 通讯作者: 薛海锋 E-mail:xuehf.zhlh@sinopec.com

PRACTICE OF REVAMPING DIESEL HYDROTREATING UNIT FOR NAPHTHA HYDROTREATING

  • Received:2013-08-06 Revised:2013-12-16 Online:2014-04-12 Published:2014-03-24

摘要: 介绍了中国石化镇海炼油化工股份有限公司柴油加氢装置扩能改造为处理焦化汽油、非芳石脑油的石脑油混合加氢装置后的运行情况、存在的一些问题及解决措施。运行结果表明:在高压分离器压力3.40 MPa、第一反应器温度222 ℃、第一反应器温度266~267 ℃、体积空速1.85 h-1的条件下,精制石脑油产品硫质量分数小于200 ?g/g,能满足乙烯装置石脑油原料的要求和大负荷生产的实际需求;装置总体改造效果较好,反应、分馏及脱硫系统均能保持平稳运行;对于影响装置平稳运行和产品质量的一些问题,经过装置消缺和操作调整后,基本得到解决。

Abstract: The operation of diesel hydrogenation unit expansion revamping for hydroprocessing the mixed feed of coker gasoline (naphtha) and non-aromatic naphtha were introduced. Problems during the operation and measures were discussed and proposed. The practices indicate that at the conditions of high separator pressure 3.40 MPa, reaction temperature of R1/R2 222℃/266~170℃,LHSV1.85 h-1,the sulfur content in the refined naphtha is less than 200 ?g/g, meeting the requirements for ethylene production and large load production as well. All transformation reaction, fractionation and desulfurization system can keep running smoothly. Some of the issues affecting the smooth operation of the device and product quality, after eliminating defects and operational adjustment, are basically resolved.