石油炼制与化工 ›› 2014, Vol. 45 ›› Issue (4): 82-84.
• 加工工艺 • 上一篇 下一篇
王航空,肖知俊,邢宇,闫晓荣
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摘要: 总结了中国石油克拉玛依石化公司1.5 Mt/a延迟焦化装置汽油终馏点调整的实践经验。在焦化汽油终馏点调整到小于180 ℃的过程中,存在柴油系统超负荷、分馏塔塔顶循环回流泵抽空及塔盘结盐等问题,通过优化调整柴油系统流程、增加塔顶循环脱水罐及塔盘定期除盐等措施,有效地控制了柴油系统的负荷,降低了柴油外送温度,解决了塔顶循环泵抽空及塔盘结盐的问题,使汽油终馏点调整无负面影响,满足了焦化汽油单独加氢作重整料的要求,优化了产品分布,保证了装置的安、稳、优运行。
Abstract: The operation experience of adjusting end-point of delayed coking gasoline of 1.5Mt/a delayed coking unit in Karamay Petrochemical Corp is summarized. The issues during the adjustment are discussed in terms of diesel system overloading, top circulating reflux pump exhausting and salt deposition on column trays. It is proved that the above issues could be handled appropriately by optimizing diesel process flowsheet, adding top circulating water sump,and cleaning tray periodically. As a result, the coking gasoline end point could be controlled under 180 ℃ and used as the feed for reforming. The diesel yield increases by 3.45% as well as higher diesel to gasoline ratio.
王航空 肖知俊 邢宇 闫晓荣. 延迟焦化装置汽油终馏点调整中存在的问题及对策[J]. 石油炼制与化工, 2014, 45(4): 82-84.
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