石油炼制与化工 ›› 2015, Vol. 46 ›› Issue (11): 42-45.
• 加工工艺 • 上一篇 下一篇
郑海,王永成
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摘要: 针对中国石化青岛炼油化工有限责任公司(简称青岛炼化)1.8 Mt/a连续重整装置二甲苯塔塔底的C9+芳烃终馏点高达250 ℃导致汽油馏分终馏点超标的问题,对二甲苯塔实施了技术改造,增设二甲苯塔侧线气相抽出流程,侧线抽出组分直接作为汽油调合组分,塔底重组分作为柴油调合组分。结果表明,该技术方案可有效脱除C9+芳烃中的重组分,大幅降低重整汽油的终馏点。
Abstract: The end point of C9+ distillates at the xylene tower bottom of the1800k/a continuous catalytic reforming unit in SINOPEC Qingdao Petrochemical Company was about 250 ℃, resulting in overstandard end point of naphtha. To solve the problems, a vapor-phase stream side-draw pipe was added to the xylene tower. The vapor-phase stream was used as a fraction of gasoline blending component directly. The bottom fraction of the tower was used as a fraction of the diesel oil blending. The results indicate that the measures can effectively remove the heavy components in C9+ fraction and reduce the end point of the naphtha.
郑海 王永成. 二甲苯塔侧线气相抽出降低汽油馏分终馏点[J]. 石油炼制与化工, 2015, 46(11): 42-45.
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