石油炼制与化工 ›› 2015, Vol. 46 ›› Issue (5): 39-44.

• 加工工艺 • 上一篇    下一篇

C5、C6异构化装置升级改造技术方案

吴惜伟1,张秋平2,于中伟2   

  1. 1. 中国石化湛江东兴分公司
      2. 中国石化石油化工科学研究院
  • 收稿日期:2014-11-24 修回日期:2014-12-12 出版日期:2015-05-12 发布日期:2015-04-21
  • 通讯作者: 张秋平 E-mail:zhangqp2.ripp@sinopec.com

C5, C6 ISOMERIZATION UNIT UPGRADE TECHNOLOGY

  • Received:2014-11-24 Revised:2014-12-12 Online:2015-05-12 Published:2015-04-21
  • Contact: Qiuping Zhang E-mail:zhangqp2.ripp@sinopec.com

摘要: 中国石化湛江东兴分公司原C5、C6异构化装置采用中国石化石油化工科学研究院(石科院)开发的中温沸石型异构化催化剂,为“脱异戊烷塔+异构化反应”流程 ,可生产RON为82的C5、C6异构化汽油。为适应车用汽油升级的需要,拟采用石科院开发的固体超强酸异构化技术对装置进行技术升级改造,以提高异构化汽油的辛烷值。对两种C5、C6异构化技术的流程、催化剂用量、异构化产物辛烷值、设备、能耗等进行对比,并对改造后的效果进行模拟分析,结果表明,在原流程不变的情况下,可以以较小的改造费用升级为固体超强酸异构化技术方案,在异构化催化剂的用量大幅减少的同时得到RON为84.2的异构化产品。

Abstract: Zhanjiang Dongxing Petroleum Refinery Ltd. SINOPEC adopted a “de-isopentane tower+ isomerization reaction” process to produce C5, C6 isomerization gasoline with RON 82 using moderate temperature zeolite-based C5,C6isomerization catalyst developed by RIPP. In order to upgrade gasoline, the unit upgrading was conducted to use RIPP`s solid superacid isomerization catalyst to improve the ON of isomerate. Two kinds of C5, C6 isomerization processes were simulated to compare the effect of catalyst dosage, RON of isomerate, equipment, and energy consumption on transformation results. The results show that using the original process with little changes and low cost, the unit can produce RON 84.2 isomerate with much less solid superacid isomerization catalyst dosage.