石油炼制与化工 ›› 2024, Vol. 55 ›› Issue (11): 100-105.

• 节能减排 • 上一篇    下一篇

加氢装置开工预硫化期间加热炉烟气SO2浓度超标原因分析及对策

刘荣1,浦宁2,周景茹3,朱清玥3,何豪健1,任亮2   

  1. 1. 中国石化上海石油化工股份有限公司炼油部
    2. 中石化石油化工科学研究院有限公司
    3. 中国石化上海石油化工股份有限公司质量管理中心
  • 收稿日期:2024-04-24 修回日期:2024-07-23 出版日期:2024-11-12 发布日期:2024-10-29
  • 通讯作者: 任亮 E-mail:ren-liang.ripp@sinopec.com

ANALYSIS AND SOLUTION MEASURES OF EXCESSIVE SO2 CONCENTRATION IN FLUE GAS OF HEATING FURNACE DURING THE PRESULFIDING PERIOD OF HYDROTREATING UNIT


  • Received:2024-04-24 Revised:2024-07-23 Online:2024-11-12 Published:2024-10-29

摘要: 在加氢装置开工预硫化期间,加热炉烟气SO2浓度多次异常上升甚至超标,企业被迫停止回收火炬气。通过对开工预硫化期间循环氢、低压分离器气和火炬气中硫化物的类型和含量进行分析,推测是因为所使用的硫化剂二甲基二硫醚分步分解产生的甲硫醇和甲硫醚随着火炬气进入燃料气系统,甲硫醇、甲硫醚燃烧生成的SO2导致加热炉烟气中的SO2浓度超标。针对这一问题,可以通过优化火炬气脱硫溶剂、使用器外真硫化催化剂、使用新型硫化剂等方式解决。

关键词: 加氢装置, 预硫化, 加热炉烟气, 二氧化硫, 脱硫溶剂, 器外真硫化, 新型硫化剂

Abstract: During the presulfiding period of the hydrotreating unit, the SO2 concentration in the flue gas of the heating furnace has increased abnormally or even exceeded the standard, and enterprise was forced to stop the recovery of torch gas. By analyzing the sulfur types and content of circulating hydrogen, low separation gas and flare gas during the start-up of presulfiding period, it is speculated that the methyl mercaptan and methyl sulfide produced by the step-by-step decomposition of the sulfurizing agent enter the fuel gas system with the flare gas. The SO2 produced by the combustion of methyl mercaptan and methyl sulfide causes the concentration of SO2 in the flue gas of the heating furnace to exceed the standard. This problem can be solved by optimizing the desulfurization solvent of torch gas, using ex-situ true sulfidization catalyst and using new sulfiding agents.

Key words: hydrotreating unit, presulfiding, flue gas of the heating furnace, SO2, desulfurization solvent, ex-situ true sulfidization, new sulfiding agent