石油炼制与化工 ›› 2026, Vol. 57 ›› Issue (5): 18-23.

• 加工工艺 • 上一篇    下一篇

催化裂解汽油选择性加氢生产芳烃抽提原料(RGTA)技术开发及应用

张登前1,翟维明1,李桂军2,习远兵1,刘锋1,徐凯1,甘凌峰2   

  1. 1. 中石化石油化工科学研究院有限公司
    2. 中国石化安庆分公司
  • 收稿日期:2025-10-17 修回日期:2025-11-26 出版日期:2026-05-12 发布日期:2026-04-24
  • 通讯作者: 习远兵 E-mail:xiyb.ripp@sinopec.com
  • 基金资助:
    国家重点研发计划

DEVELOPMENT AND APPLICATION OF SELECTIVE HYDROGENATION TECHNOLOGY FOR DEEP CATALYTIC CRACKING GASOLINE TO PRODUCE AROMATICS EXTRACTION FEEDSTOCK (RGTA)


  • Received:2025-10-17 Revised:2025-11-26 Online:2026-05-12 Published:2026-04-24

摘要: 开发了催化裂解汽油选择性加氢生产芳烃抽提原料(RGTA)技术,研制了低芳烃饱和率催化剂RGA-1,与参比剂相比,在深度脱氮时,RGA-1催化剂芳烃饱和率更低。工业应用结果表明: RGTA技术处理硫质量分数为840 μg/g、氮质量分数为35.7 μg/g、烯烃质量分数为18.3%、芳烃质量分数为57.5%的重油催化裂解汽油时,加氢产物芳烃饱和率为3.83%,产物中C6~C8馏分的硫、氮质量分数均小于1.0 μg/g; 该技术芳烃饱和率低,长周期运转稳定,产品满足后续芳烃抽提装置进料要求。

关键词: 催化裂解汽油, 选择性加氢, 芳烃抽提, 脱氮, 芳烃饱和率

Abstract: The selective hydrogenation technology for catalytic pyrolysis gasoline to produce aromatics-extraction feedstock (RGTA) was developed. A low-aromatics-saturation catalyst, RGA-1, was developed, compared with a reference catalyst it exhibits a markedly lower aromatics saturation while achieving deep denitrogenation. Commercial application results demonstrated that, as processing heavy catalytic pyrolysis gasoline feedstock with a sulfur mass fractions of 840 μg/g, a nitrogen mass fractions of 35.7 μg/g, an olefin mass fractions of 18.3%, and an aromatica mass fractions of 57.5%, the aromatics saturation rate of the hydrogenated product was 3.8%. The mass fractions of sulfur and nitrogen in the C6—C8 fraction of hydrogenated product were both less than 1.0 μg/g. The technology showed excellent selectivity, low aromatics saturation rate, stable long-term operation, and produces feedstock meeting the requirements for subsequent aromatic extraction units.

Key words: deep catalytic cracking gasoline, selective hydrogenation, aromatics extraction, denitrogenation, aromatics saturation rate