石油炼制与化工 ›› 2026, Vol. 57 ›› Issue (5): 24-31.

• 加工工艺 • 上一篇    下一篇

炼油厂碳四萃取精馏和加氢组合工艺开发与应用

马立国   

  1. 中国石化工程建设有限公司
  • 收稿日期:2025-12-22 修回日期:2026-01-12 出版日期:2026-05-12 发布日期:2026-04-24
  • 通讯作者: 马立国 E-mail:maliguo.sei@sinopec.com
  • 基金资助:
    中国石化科技开发合同

DEVELOPMENT AND APPLICATION OF COMBINED PROCESS OF EXTRACTIVE DISTILLATION AND HYDROGENATION OF REFINERY C4

  • Received:2025-12-22 Revised:2026-01-12 Online:2026-05-12 Published:2026-04-24

摘要: 针对炼油厂碳四资源高价值化工利用不足的问题,开发了烷烃/烯烃萃取精馏与低反应温升的加氢工艺的耦合工艺,对炼油厂的碳四资源进行分级利用。应用夹点技术对加氢工艺换热流程进行优化,实现了正常生产时停用加热炉,利用低温热大幅节省蒸汽消耗。采用该技术建成的600 kt/a装置一次性开车成功,反应器负荷最高可达到120%,产品异丁烷纯度(w)为99.9%,硫质量分数小于0.5 μg/g;正丁烷产品纯度为97%,硫质量分数小于0.5 μg/g;富丁烯纯度为95%,实际能耗大幅低于设计值,装置运行稳定。表明该技术实现了炼油厂碳四资源有效利用,为企业创造了较高效益。

关键词: 炼油厂, 萃取精馏, 加氢, 异丁烷, C4烯烃

Abstract: In order to solve the problem of insufficient utilization of C4 resources as high-value chemicals in refineries, the coupling process of alkane/olefin extractive distillation and low reaction temperature rise hydrogenation process was proposed, and the C4 resources in a refinery were classified and utilized. The pinch technology is applied to optimize the heat exchange process, and realize the normal production and shutdown of the heating furnace, which can greatly save steam consumption by using low-temperature heat. The 600 kt/a unit built by this technology has been successfully started up at one time, the maximum reactor load can reach 120%, the purity (mass fraction) of isobutane product is 99.9% with sulfur mass fraction less than 0.5 μg/g, the purity of n-butane product is 97% with sulfur mass fraction less than 0.5 μg/g, the purity of rich butene is 95%, the actual energy consumption is significantly lower than the design value, and the unit operates stably. It shows that the technology realizes the effective utilization of C4 resources in refineries and creates higher benefits for enterprises.

Key words: refinery, extractive distillation, hydrogenation, isobutane, C4 olefin